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induction

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TUP49 Simulations of the Ion-Hose Instability for DARHT-II Long-Pulse Experiments simulation, linac, electron, resonance 381
 
  • K. C. D. Chan, C. Ekdahl
    LANL, Los Alamos, New Mexico
  • C. Genoni, P. Hughes
    MRC, Albuquerque, NM
  Ion-hose effect has been described extensively in literatures. Computer simulations of the effect typically use particle-in-cell (PIC) computer codes or codes using the spread-mass formulation [1]. PIC simulations, though offering more reliable results, will require extended running time in large computers To support commissioning experiments in the DARHT-II induction linac in Los Alamos National Laboratory, we have modified a spread-mass code so that we can survey quickly the parameter space for the experiment. It can also be used to provide quick answers during experiment. The code was originally written by Genoni from Mission Research Corporation (MRC) for constant linac parameters. We have modified it so that parameters can have dependence along the length of the linac. In this paper, we will describe simulation results using this code for the DARHT-II commissioning experiment and also our benchmarking results comparing to LSP, a PIC code from MRC.

[1] T. C. Genoni and T. P. Hughes, "Ion-hose instability in a long-pulselinear induction accelerator", PRST-AB, 6, 030401 (2003)

 
 
THP42 NLC Hybrid Solid State Induction Modulator klystron, pulsed-power, controls, vacuum 697
 
  • R.L. Cassel, M. Nguyen, G.C. Pappas, J.E. deLamare
    SLAC, Stanford
  • C. Brooksby, E. Cook, J. Sullivan
    LLNL, Livermore
  The Next Linear Collider accelerator proposal at SLAC requires a high efficiency, highly reliable, and low cost pulsed power modulator to drive the X-band klystrons. The original NLC envisions a solid state induction modulator design to drive up to 8 klystrons to 500 kV for 3 μs at 120 PPS with one modulator delivering greater than 1,000 MW pulse, at 500 kW average. A change in RF compression techniques resulted in only two klystrons needed pulsing per modulator at a reduced pulse width of 1.6 μsec or approximately 250 MW of the pulsed power and 80 kW of average powers. A prototype Design for Manufacturability (DFM) 8-pack modulator was under construction at the time of the change, so a redirection of modulator design was in order. To utilities the equipment which had already be fabricated, a hybrid modulator was designed and constructed using the DFM induction modulator parts and a conventional pulse transformer. The construction and performance of this hybrid two klystron Induction modulator will be discussed. In addition the next generation DFM induction modulator utilizing a ten turn secondary and fractional turn primary transformer well be presented.